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Andy7:
04 Jul 2020 13:16:48
VIDEO or it didn't happen!! :) Nice going though, keep it up!
Bad Raven:
02 Jul 2020 19:46:48
 ~~
whoelseisbored (LiamHowe89):
02 Jul 2020 17:45:19
Sounds basic but I'm happy with it  :laugh:
whoelseisbored (LiamHowe89):
02 Jul 2020 17:45:05
Managed a split s :D
badger1:
28 Jun 2020 12:29:49
BF GPS Rescue mode configured - what could possibly go wrong?   :o
badger1:
27 Jun 2020 21:07:37
and can't make it back to where you take off from   :laugh:
badger1:
27 Jun 2020 21:07:04
it's too windy if you fly downwind
Bad Raven:
27 Jun 2020 20:51:32
I have done Dynamic Soaring in over 55mph, and quad flying in over 25mph with the right equipment.
whoelseisbored (LiamHowe89):
26 Jun 2020 16:44:24
How windy is too windy? :hmm:
whoelseisbored (LiamHowe89):
25 Jun 2020 22:58:29
YASSSS!! Flew a full 2 packs and no motors going nuts on me!  :D
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3d - Printworx

Printing 3d Forum

Rabbit FC and DX6i

Started by Angry hornet, Sunday,May 18, 2014, 09:18:21

Previous topic - Next topic

Angry hornet

Sunday,May 18, 2014, 09:18:21 Last Edit: Sunday,May 18, 2014, 09:21:36 by Angry hornet
I am hoping there is a solution to my problem.

I have the Rabbit FC sitting on X525 frame, I brought it second hand :slap:

I have been able to run through the calibration process with all the correct beeps but when I try and take off it just flips over. I am guessing that I have the channels mixed up.

I am using the Jacked Rabbit GUI and input channels all correspond to the TX action,  what should the output Channel variables be doing?

:banghead:

PS also I am using V:1.212 really have no idea how to update this firmware if could help with that you will receive guru status :notworthy:


Please help!!

Angry hornet

Wow! Ok!
So I have been going through the process of elimination and found that M3 and M4 were plugged into each other';s ports...... Oops! :frantic:

I have had a couple of flights/hovers now and really enjoying it a lot!  ::)

I am having some stability problems but figure it';s just fine tuning the stability controls ect..

Could anyone give me a bit of advice on what they have theirs set at?

Also has anyone had problems with the ultrasonic module not initialising and stoping the rabbit from discovering it or going into breathing mode?

I have had to uncheck it in the GUI this allows me to get the rabbit into the breathing mode.

Do you think it';s the rabbit FC or the Ultrasonic module?

Kind regards
Angry hornet   :help:







JAB1a

I used the Rabbit for about 3years, its an excellent FC!.

Get rid of that ultrasonic, only good under 2.5meters and does not work (almost at all) on grass I found. The standard settings on the FC are perfect, make sure all your arms are straight and make sure all your motors are pointing straight up and form a perfect square (shaft to shaft). Then make sure your CG is spot on and the rabbit will be your best friend, alter any of those and you will be in for a bumpy ride. Get the latest firmware installed as well, think its 1.231 (it was released about april 2013 I think), you might need to short the ';reset'; pins while you do the update coming from 1.212 otherwise it will fail at about 58%.

The board is awesome and I hope you have fun. I am still using my modified X525 frame on my big quad but its now using a Full Naze32 instead.