Welcome to Multi-Rotor UK. Please login or sign up.

Tuesday,August 20, 2019, 21:56:26

Login with username, password and session length

Shoutbox

Andy7:
19 Aug 2019 09:14:20
Good for you!  ~~
DarkButterfly:
18 Aug 2019 19:13:57
Had another negative encounter, it's been a few years since the last one, just an uneducated ******, going on about drones being illegal yada yada yada.    :-/
Still that didn't spoil my flying time, had an absolute blast  ~~
Gaza07:
07 Aug 2019 19:52:01
ooooh mrs jones  :D
hoverfly:
30 Jul 2019 15:26:34
D.B. you tightwad.. :cool:
atomiclama:
29 Jul 2019 20:14:10
DB that just means you have shed loads of props in the first place ;-)
DarkButterfly:
29 Jul 2019 18:53:33
Just had a thought, even with all the crashing I've done, I haven't bought any replacement props in over a year ~~
ched:
09 Jul 2019 19:45:42
May the sun shine and winds be light for BFU#8. Son't forget lots of vids for those of us unable to attend.  :D
Gaza07:
09 Jul 2019 18:10:30
Hope you all have a great day  :beer2:
Andy7:
09 Jul 2019 14:05:28
BFU#8 details locked in for this saturday - see the head of the forum thread for all details.
hoverfly:
05 Jul 2019 21:51:05
Good for genital warts as well......or so I'm told.. :hmm
Members
  • Total Members: 8066
  • Latest: badger1
Stats
  • Total Posts: 196558
  • Total Topics: 19801
  • Online Today: 50
  • Online Ever: 530
  • (Tuesday,June 26, 2012, 08:34:46 )
Users Online
Users: 0
Guests: 42
Total: 42

Theme Changer





3d - Printworx

Printing 3d Forum

X580 multirotor first build help!

Started by mfc123, Saturday,September 28, 2013, 01:21:24

Previous topic - Next topic

mfc123

Hi!

This is my first build and I';m new in the world of RC and Quadcopters!

My current build is :

Hobbyking X580 frame
4 x HexTronik DT750 Brushless Outrunner 750kv
4 x HobbyKing 20A BlueSeries Brushless Speed Controller
Crius AIO Pro V2 with MegapirateNG
NEO-6M GPS Module
Turnigy 9x with 8-channel transmitter module DJT-II (V2)
8-channel receiver D8R-II Plus

I have mounted all and flashed the MegapirateNG with arduino and configured all.

Tested the motor rotation and corrected all like in the arducopter tutorial.

Then installed the Mission Planner and connecter to test the sensors, all are Ok including GPS.

Next I have done the auto calibration of the ESC...

The next step was to finally test how it flies... It';s when it all gone wrong!!

My quad on the take-off was flying real bad and I lost it for 10 days...I searched it for 10 days and found it :) lol

Can you please tell me what went wrong??

Here are some pics of my quad and the crash video :/

https://www.dropbox.com/s/df0u79hqmqpdjya/20130903_235411.jpg

https://www.dropbox.com/s/ray9iyykdmj7js4/20130904_122720.jpg

Video :

flybywire

Wednesday,October 02, 2013, 12:58:00 #1 Last Edit: Wednesday,October 02, 2013, 18:36:59 by flybywire
Sorry to hear you';re having probs. mfc123  :banghead:, I know B***** all about the Megapirate I';m afraid, but I';m sure somebody will be along shortly to help you out!  THey';re like that on this forum  :smiley:

Fly-aways are scary things, hope you get it sorted sometime soon

Andy
Blog: http://ajwillis303.wix.com/stuff
The spiritual home of fpv large
Keep it emax, capiche?
Hardware? sure, I got hardware!

barneyg

First thought is your PID';s are out ... when I used MPNG I had to use P=0.07 ish and D=0.004 ish (If I remember right) ... but I';m sure that some more experienced people will be along soon :)