Well got it all wire up last night, loaded BF RC12, configured it and pressed arm.
it almost shook it's self apart and the smell of things getting hot. Really must remember not to use the default PIDs, way too high.
Halved everything and tried again, much better.
First flight this morning and all is well.
Bit of resonance at a particular motor speed that I have never seen before. Ah well something to sort out.
Now to move FPV gear over.
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Yes it is held together with electrical tape